01-10-2020, 09:49 AM | #1 |
Join Date: Jan 2020
Posts: 5
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Apollo DB-36 new carb and revving issues...
I recently picked up a 2017 DB-36. been working on it the past few days and finally got my carb (mikuni clone off amazon, 30mm, vm26) and jets in yesterday. last night i went ahead and installed the new carb and switched out the 100 jet for the 110 jet, and pieced everything back together. whenever i switched the carb over i used the new parts for everything, including the spring for the throttle cable. the only part i did not use was the new elbow fitting into the head.
After getting it started and adjusting the fuel screw on the side of the carb, it idles really well. My only problem now is whenever it is idling and you rev it sometimes it will stay at a higher RPM anywhere from 5-30 seconds. I have not adjusted the air screw on the bottom of the carb, but I do not know if i need to do that. also i am located in baton rouge, Louisiana and from my understanding the 110 main jet is what i should be using if not the 115. |
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01-10-2020, 09:57 AM | #2 |
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Join Date: Oct 2016
Location: Houma, La.
Posts: 11,707
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Sounds like you either have a intake leak or need to adjust the idle mixture screw on the bottom. Check to make sure the gaskets' oring and intake are not damaged. BTW Welcome aboard to another Louisiana neighbor. I'm down in Houma.
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2024 Linhai 300 ATV 4x4 2023 Lifan Lycan 250 Chopper 2023 Venom Evader 2022 Lifan KPX250 2020 Kawasaki Vulcan S (Sold) 2004 Honda ST 1300 2016 Black Hawk 250 (sold) Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster 2016 Cazador180 XL 2014 Coolster150 JerryHawk250.com My YouTube Channel |
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01-10-2020, 10:11 AM | #3 | |
Join Date: Jan 2020
Posts: 5
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Quote:
when i get off work today ill try adjusting the mixture screw on the bottom. i ended up using the old gaskets and orings from the manifold because the new ones did not fit the old manifold. the carb itself had a new oring on it. |
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01-10-2020, 10:23 AM | #4 |
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Join Date: Oct 2016
Location: Houma, La.
Posts: 11,707
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I've only seen one other Chine bike around here and it was an old beat up one but was still running.
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2024 Linhai 300 ATV 4x4 2023 Lifan Lycan 250 Chopper 2023 Venom Evader 2022 Lifan KPX250 2020 Kawasaki Vulcan S (Sold) 2004 Honda ST 1300 2016 Black Hawk 250 (sold) Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster 2016 Cazador180 XL 2014 Coolster150 JerryHawk250.com My YouTube Channel |
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01-10-2020, 02:49 PM | #5 |
Join Date: Mar 2009
Location: Sardis, BC, Canada
Posts: 25,977
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I'm with Jerry that it could be a vacuum leak; I've seen that on two different China machines. In my case, it was where the intake tube met the head. The o-ring groove was cut too deeply in one case, meaning that the o-ring could not properly squish against the aluminum. In the other case, the o-ring had slipped out of the groove on assembly at the factory, so only part of it was installed properly.
With the groove that was cut too deeply, I used two O-rings to temporarily solve it. The proper fix is to sand down the aluminum surface (ideally on a bench-top belt sander or on a milling machine if you have access) to the point where the groove is much shallower. With the one where the o-ring had popped out on assembly, I just replaced the o-ring. In both cases, revs settled quickly after repairs.
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Weldangrind "I figure I'm well-prepared for coping with a bike that comes from the factory with unresolved issues and that rewards the self-reliant owner." - Buccaneer |
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01-11-2020, 03:39 PM | #7 |
Join Date: Jan 2020
Posts: 5
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I just bypassed it and put the gasket on so now that manifold elbow bolts directly to the carb. Not sure what that shim was really there for. Any ideas?
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01-11-2020, 03:56 PM | #8 | |
Join Date: Jan 2012
Location: ChCh , NZ
Posts: 2,265
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Quote:
the idea of it is to stop / reduce heat transfer and vibration to the carb... ..
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01-13-2020, 12:08 PM | #9 |
Join Date: Mar 2009
Location: Sardis, BC, Canada
Posts: 25,977
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^ this.
It's often called a phenolic spacer.
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Weldangrind "I figure I'm well-prepared for coping with a bike that comes from the factory with unresolved issues and that rewards the self-reliant owner." - Buccaneer |
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01-16-2020, 04:47 PM | #10 |
Join Date: Jan 2020
Posts: 5
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i repaired the spacer as best i could using some hightemp epoxy. new one is on the way along with a new, longer fuel mixture screw with the finger dial on the bottom. right now it runs fine and idles fine, but when you rev it they still stay high, higher than before. I flipped the choke switch, causing it to rev high and then turned the choke off and it also stayed revving high. I figure doing that eliminates the chance of there being a throttle cable issue.
Hopefully the new spacer will fix this issue, along with the new screw that will make it easier to adjust the fuel/air mixture. |
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