04-12-2019, 11:50 PM | #16 | |
Join Date: Jan 2012
Location: ChCh , NZ
Posts: 2,266
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$64 helmet bought on line... you don't value you head to highly ? most parts of the body can be repaired , brain damage is for ever.. .
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09 XT660R ... 06 TTR250 ... 80 Montesa H6 125 Enduro... 77 Montesa Cota 348 MRR "Malcom Rathnell Replica"... Current resto projects.. 81 Honda CT110... 80 Kawasaki KL250A1... 11 Husaburg TE125 enduro... "sold" along with another 31... Lifan 125 Pitbike.. "stolen" ... KIWI BIKER FORUM...... http://www.kiwibiker.co.nz/forums/content.php All the best offroad rides in NZ... http://www.remotemoto.com/ E-mail... xtpete1@gmail.com |
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04-13-2019, 01:42 AM | #17 |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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You're right, even though it's DOT certified I probably shouldn't trust it. I'll just go back to wearing the cheap safety glasses and hope for the best.. Hahaha!
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04-13-2019, 04:17 AM | #18 |
Join Date: Nov 2016
Location: robertsdale alabama usa
Posts: 1,007
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hmmm mine was $10 and said for novelty use only!
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1991 harley heritage softail classic 2016 hawk kaw h1 400 tripple 13' long chopper in progress 2009 johnny pag bar hog 2004 hd electra glide ultra classic shriner edition 1997 harley davidson 1200 sportster 1972 harley davidson amf sx250 |
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04-13-2019, 10:37 PM | #19 | |
Join Date: Aug 2018
Posts: 29
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I have a dumb question but I bought some handle bar sliders/weights and I couldn't figure out how to get the bolted on I figure they would bolt on however the bark Buster's do just wondered where the bolt goes into on the the handle bar.
Thanks Fantastic Moto
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Fantastic Moto 2017 Coolster Pit Bike (SOLD) 2015 Green Hawk(Air box opened,Alarm Disabled, China Mikunni carb,105 main jet) (SOLD) 2018 Black Hawk(Air Box opened, Alarm Disabled,China Mikunni Carb,110 Main Jet,Cut out Cat,) Quote:
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04-14-2019, 11:48 AM | #20 |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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The helmet worked out great, I wore it for hours yesterday on a 140 mile ride. It fits snugly and the outer visor really blocks out the wind and didn't distort my vision, didn't try the inner visor yet.
The gas gauge started working after I fully filled the tank, but reads empty when you get to half a tank which lead to an unnecessary fuel stop lol. The bike actually broke in some during the ride. By the end of the day it ran better and stronger and went 10mph faster. And finding neutral was easier. Still not happy with the carb, seems lean and snappy up to 3/4 throttle and boggy from 3/4 to wide open throttle. Currently I'm at 2.25 turns out on the mixture screw, 2 washers on the needle and a 115 main jet. So if the rain lets up today I'm gonna drill the pilot to .45mm, take the mixture back to 1.5 turns out and may go back to the 110 main jet if it still feels boggy after I do the airbox mod. Always tinkering lol. Last edited by OneLeggedRider; 10-30-2019 at 02:58 AM. |
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04-14-2019, 12:13 PM | #21 | |
Join Date: Apr 2017
Location: Omaha, NE
Posts: 8,110
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Quote:
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Hawk Information and Resource guide: http://www.chinariders.net/showthread.php?t=20331 2018 Hawk 250 - Full Mod list here. http://www.chinariders.net/showpost....62&postcount=1 2024 Royal Enfield Shotgun 650 https://chinariders.net/showthread.php?t=34124 |
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04-14-2019, 02:10 PM | #22 | |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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04-17-2019, 11:43 AM | #23 |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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Did the airbox mod yesterday but there was no discernible difference when I test rode it. On a flat and straight stretch of road down by the river I can attain and maintain 67mph at 3/4 throttle. At wide open throttle I can only achieve 62mph and it misses and bogs. And it's more pronounced on a steep hill in any of the top 3 gears. It pulls strong and hard at 3/4, at WOT it bogs, loses speed and you have to downshift. Clearly the 115 main jet is too big. I'm gonna try the 110 and see how it performs, but I still think the pilot is too small and needs to be drilled.
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04-17-2019, 01:01 PM | #24 |
Moderator
Join Date: Oct 2016
Location: Houma, La.
Posts: 11,739
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Before the head work I was running a 120 main on the stock PZ30 with the gutted stock exhaust and air box mod in the cool months and 115 in the summer which was a tad lean. The 110 may be on the lean side. Hope you get it sorted out.
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2024 Linhai 300 ATV 4x4 2023 Lifan Lycan 250 Chopper 2023 Venom Evader 2022 Lifan KPX250 2020 Kawasaki Vulcan S (Sold) 2004 Honda ST 1300 2016 Black Hawk 250 (sold) Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster 2016 Cazador180 XL 2014 Coolster150 JerryHawk250.com My YouTube Channel |
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04-17-2019, 02:39 PM | #25 |
Join Date: Apr 2017
Location: Omaha, NE
Posts: 8,110
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Just a suggestion, since you are still running the stock intake. If that intake tube has a Kink in it, use a hose clamp and/or strong zip ties to try and get the kink out of it. I noticed a distinct difference with my first Hawk after having made that little adjustment. Mine was pretty severe and was basically reducing the intake size down by half.
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Hawk Information and Resource guide: http://www.chinariders.net/showthread.php?t=20331 2018 Hawk 250 - Full Mod list here. http://www.chinariders.net/showpost....62&postcount=1 2024 Royal Enfield Shotgun 650 https://chinariders.net/showthread.php?t=34124 |
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04-17-2019, 03:49 PM | #26 | |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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04-17-2019, 05:00 PM | #27 |
Join Date: May 2018
Posts: 64
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Mine had a pretty bad kink too. Definitely noticed the difference after switching to pod filter.
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2017 RPS Hawk. Mikuni carb, 117.5 main, 25 pilot. Foam filter. NGK plug. Upgraded exhaust. 17/45 sprockets. Digital speedo. Full LED all around. U5 handlebar spot lights. 1982 Yamaha XJ1100 Maxim |
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04-17-2019, 05:11 PM | #28 |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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Not the problem. I warmed it up and took the intake completely off the carb. It may have ran slightly better at WOT, but not much. Still bogging after 3/4 throttle.
Also I know from working on the flow bench you can take a round orifice and compress it to 60% of it's diameter and not really affect flow. If anything it might affect turbulence which could be bad on the intake side of the venturi and may be beneficial on the head side. |
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04-17-2019, 06:28 PM | #29 | |
Join Date: Apr 2017
Location: Omaha, NE
Posts: 8,110
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If you do drill the stock pilot I am rather curious as to your results. Comparing our two builds is like apples to oranges obviously, but there are a lot of other factors at play (head, much larger main jet< etc). I tinkered more with my idle mixture and idle speed today and I think I finally found my happy place just shy of 2 turns out. Cold starts with no choke and holds a dead steady idle.
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Hawk Information and Resource guide: http://www.chinariders.net/showthread.php?t=20331 2018 Hawk 250 - Full Mod list here. http://www.chinariders.net/showpost....62&postcount=1 2024 Royal Enfield Shotgun 650 https://chinariders.net/showthread.php?t=34124 |
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04-17-2019, 07:14 PM | #30 |
Join Date: Nov 2018
Location: Stockport, Oh.
Posts: 1,442
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This isn't my first rodeo and I'm sure it will be resolved soon. I actually made a generator run using a plastic citrus fertilizer sprinkler for 6 months. My worst carb was experience was replacing a motor in my '76 CJ 5 with a newer emissions motor. Seemed like no matter what I did it wasn't right, but I eventually figured that out too.
Drilling the pilot is scary and it's something we were taught never to do in school. But considering we can't get a bigger pilot which I know it needs.. And old school racers did it on the regular. They even bored the venturi though so I wonder how much they understood about fluid dynamics lol. I'm thinking drill the pilot to.45mm, and go to the 110 main jet. If that's not satisfactory remove the 2 washers from the needle and turn the mixture down to 1.25 turns out. If that doesn't work I'll simply replace it with a nicer carb. I'm not rich but parts for these things cost almost nothing. Ask me how much I got in my Scrambler or how much I paid for the UFO carb. Big difference. |
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