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Old 07-31-2019, 01:13 PM   #31
Vtunimog   Vtunimog is offline
 
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Quote:
Originally Posted by JerryHawk250 View Post
It could be a coil going bad. Mine had started acting up so I swapped it out to a coil on plug. Much stronger spark.



do you have a post on that ?


 
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Old 07-31-2019, 01:20 PM   #32
JerryHawk250   JerryHawk250 is offline
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Quote:
Originally Posted by Vtunimog View Post
do you have a post on that ?
Links in my signature along with my other mods.
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Old 08-06-2019, 01:00 AM   #33
SecondHandHawk   SecondHandHawk is offline
 
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Hey guys.
Sorry to but in but I recently tuned my stock carb with some trial and error. Everything is fine for me just running a little rich.
I have searched a bit but cannot find an average mpg for the hawk. What do most riders consider a good mpg?
One other thing is after tuning my carb my hawk starts right up without using the choke at all.


 
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Old 08-06-2019, 07:32 AM   #34
JerryHawk250   JerryHawk250 is offline
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Quote:
Originally Posted by SecondHandHawk View Post
Hey guys.
Sorry to but in but I recently tuned my stock carb with some trial and error. Everything is fine for me just running a little rich.
I have searched a bit but cannot find an average mpg for the hawk. What do most riders consider a good mpg?
One other thing is after tuning my carb my hawk starts right up without using the choke at all.
I average about 65 mpg. Worst I've gotten was 62 mpg and the best was 70mpg.
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2023 Lifan Lycan 250 Chopper
2023 Venom Evader
2022 Lifan KPX250
2020 Kawasaki Vulcan S
2004 Honda ST 1300
2016 Black Hawk 250 (sold)
Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster
2016 Cazador180 XL
2014 Coolster150
JerryHawk250.com
My YouTube Channel


 
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Old 08-07-2019, 08:55 PM   #35
Vtunimog   Vtunimog is offline
 
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Update - New CDI/COIL

So splurged and bought a new CDI/COIL and airfilter from TX Powersports. Parts came in last night. Installed both - fired up and seemed to idle much smoother. Took it out it was fine for about the first mile or so. Went right back to sounding very loud, skipping on mid-acceleration and a pop now and then when hard acceleration. I am at a loss, valves - checked, CDI new , Coil - New, Sparkplug new , I have the Keihin PZ60b on, 140 main, 45 idle/1.25 turns out. Needle 3rd postion - maybe I will try second ?? or back to 4th ??



I even tried propane around the carb fittings - no luck.



one thing is the exhaust sounds a bit more well 'braappy' as my daughter put it.



acts rich on acceleration and almost like a bit lean on low end idle. very weird. I am so frustrated I also said to helll with it send me a new engine for $500 (shipping would kill me though)


 
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Old 08-07-2019, 09:02 PM   #36
JerryHawk250   JerryHawk250 is offline
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You need to go smaller on the main jet. 140 is way too big. Drop down to a 120 or 115.
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2023 Lifan Lycan 250 Chopper
2023 Venom Evader
2022 Lifan KPX250
2020 Kawasaki Vulcan S
2004 Honda ST 1300
2016 Black Hawk 250 (sold)
Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster
2016 Cazador180 XL
2014 Coolster150
JerryHawk250.com
My YouTube Channel



Last edited by JerryHawk250; 08-08-2019 at 09:21 AM.
 
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Old 08-07-2019, 09:39 PM   #37
Vtunimog   Vtunimog is offline
 
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Quote:
Originally Posted by JerryHawk250 View Post
You need to go smaller on the main jet. 140 is way too big. Drop brown to a 120 or 115.

sorry that is a typo - 120 is the main and I think 40 is the idle jet


 
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Old 08-07-2019, 10:11 PM   #38
NzBrakelathes   NzBrakelathes is offline
 
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Quote:
Originally Posted by Vtunimog View Post
skipping on mid-acceleration and a pop now and then when hard acceleration. I am at a loss, valves - checked, CDI new , Coil - New, Sparkplug new , I have the Keihin PZ60b on, 140 main, 45 idle/1.25 turns out. Needle 3rd postion - maybe I will try second ?? or back to 4th ??
140 main jet? that is massive! maybe 105-112 would be the most you should use


 
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Old 08-07-2019, 10:15 PM   #39
NzBrakelathes   NzBrakelathes is offline
 
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Quote:
Originally Posted by Vtunimog View Post
sorry that is a typo - 120 is the main and I think 40 is the idle jet
You seem to have carb issues and what you are writing is or shows the carb tuning is just way wrong.

Say no mods pilot 40-45.
Main 105 - 112
Clip in center of needle
Screw out 1.5 to 2.25 turns

That is something around where it all prob should be - vague yeah


What you've written is putting off any advise cause you seem to have stated wrong info etc


 
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Old 08-08-2019, 09:13 AM   #40
Vtunimog   Vtunimog is offline
 
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Quote:
Originally Posted by NzBrakelathes View Post
You seem to have carb issues and what you are writing is or shows the carb tuning is just way wrong.

Say no mods pilot 40-45.
Main 105 - 112
Clip in center of needle
Screw out 1.5 to 2.25 turns

That is something around where it all prob should be - vague yeah


What you've written is putting off any advise cause you seem to have stated wrong info etc

I have three carbs,

Stock PZ30 Clone, All stock no changes or upgrades - Same behavior

VM26 Clone - 115 Main/25 Idle - 4th ring needle position - 1.5-2 turns of the mixture screw. Same behavior just much much worse


Keihin PW30b (clone?). 120 Main, 40 or 45 they are not marked so I have to compare to a lower and larger numbered jet that is marked - 3rd Notch/ring on needle, 1.25 turns of the mixture screw (again on the bottom ??) Behavior noted before comes on more slowly but builds as bike heats up.

I can’t believe all three would exhibit mostly the same behavior. The VM26 was the worst of the three sputtering and more or less undrivable but at WOT when hot.

Like I said before - valves checked 2twice, new coil new CDI, New air filter , box cleaned. Did a leak test around carb/intake. Checked all electrical connections. After suffering through a no spark situation with my KLR I have gotten pretty good at checking every ground, every connector and wire.

What is left there must be something I am missing. I have had strange behavior on 2 strokes but different animal and usually it means air intrusion and a holed piston.

I do appreciate all the feedback and help. I have a mechanic who works on my snowmobiles and other small engines. I may try him as he has a great deal of experience with small carbs and issues with them. I am tempted to try another $40 Mikuni clone as my mikuni has a pinched floatbowl gasket and it seems I cannot find a replacement.

When I put the Keihin back on that was my 18th time of having the carb off and on again. Despite this annoying problem I still love the bike reminds me so much of the XR/XLT Honda’s I had as a kid.


 
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Old 08-08-2019, 10:45 AM   #41
NzBrakelathes   NzBrakelathes is offline
 
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https://rover.ebay.com/rover/0/0/0?m...2F303210660601

https://rover.ebay.com/rover/0/0/0?m...2F303210680840

Here are a couple of tuning products I sell

I suggest tuning the screw to gain best idle n back off 1/8th turn so your mixture then should be right for the pilot jet
It’s a screw driver that hooks under the carb

Most guys don’t get you need to tune by ear first as well as pull plug
I do by ear best idle n little back in


 
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Old 08-08-2019, 10:19 PM   #42
China Rider 27   China Rider 27 is offline
 
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Quote:
Originally Posted by jeffrey View Post
Is there any chance the stator could be bad or the magnetic pickup. I don't know just guessing. Seems like you tried every thing else.
I second those comments. Saw this link on no start interesting.

http://www.chinariders.net/showthrea...ghlight=stator


 
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Old 08-09-2019, 02:23 AM   #43
NzBrakelathes   NzBrakelathes is offline
 
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Originally Posted by jeffrey View Post
Is there any chance the stator could be bad or the magnetic pickup. I don't know just guessing. Seems like you tried every thing else.
Easier to swap to universal type that got a DC input - wire drops into the say brake switch - EASY WAY to see if stator or not and if solves the issue then good to go.

Or do a voltage check at red/white wire should be about 75v and rev it up till sputters see if changes


 
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Old 08-09-2019, 10:15 AM   #44
wedooit   wedooit is offline
 
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acts rich on acceleration and almost like a bit lean on low end idle. very weird. I am so frustrated I also said to helll with it send me a new engine for $500 (shipping would kill me though)[/QUOTE]

hmmm thinking out loud here..... have you done a compression test?

I also remember years ago, we had a short in the kill switch as mentioned above....

without searching above....one member here had a switch on the kickstand that was giving a problem
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Old 08-12-2019, 10:37 AM   #45
wedooit   wedooit is offline
 
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Also one legged had a post about resistor plug ....etc....check out what he found.
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