Go Back   ChinaRiders Forums > Technical/Performance > Dual Sport/Enduro
Register FAQ Community Calendar Today's Posts Search
Reply
 
Thread Tools Search this Thread Display Modes
Old 03-31-2018, 03:44 PM   #1
BMF   BMF is offline
 
Join Date: Mar 2018
Posts: 24
Backfire issues

Question, I switched out the 98 jet in my carb to a 110. I went to get my bike inspected and the guy told me my bike was running lean and causing backfire. I switched to a 105 and I still get backfire when down shifting. Should I go to a 100 jet?


 
Reply With Quote
Old 03-31-2018, 04:05 PM   #2
roundhouse   roundhouse is offline
 
roundhouse's Avatar
 
Join Date: Sep 2017
Location: N Texas
Posts: 706
your going leaner with the smaller jets. Mine pops a little bit but no back fires, I added a half turn out for a total of 2 turns to the idle mixture screw and it pops even less. I have a 120 jet in right now i think with the ebay exhaust. Stock exhaust on your bike?

sorry I am no expert, I just did what the other guys did before me and posted and adjusted a little here and there.


 
Reply With Quote
Old 03-31-2018, 05:23 PM   #3
BMF   BMF is offline
 
Join Date: Mar 2018
Posts: 24
I have the ebay exhaust. I went from a 110 to 105 to 100 and it's getting worse. So you think i should go the other way and maybe try and 115 or 120?


 
Reply With Quote
Old 03-31-2018, 06:08 PM   #4
Megadan   Megadan is offline
 
Megadan's Avatar
 
Join Date: Apr 2017
Location: Omaha, NE
Posts: 8,032
First thing to understand.

When decelerating, and the throttle below 25%, the main jet is having almost no effect on your fueling. Decel popping like you describe is from a lean pilot jet (and its related idle mixture setting), not a main jet.

Second, as already covered, the smaller the jet number, the leaner the jet. If you are already lean, you need to go larger.

Third, there are 3 different jets that affect fueling, but each has the greatest effect in a given area of the throttle position. As stated before, up to around 1/4 throttle, the pilot/slow jet is the jet to focus on. between 1/4 and 3/4 throttle, the needle jet and needle. and beyond 3/4 throttle, the main jet. All of these jets will have a small impact on the other two, but it is very minimal.

Is this on a stock carb or a Mikuni?
__________________
Hawk Information and Resource guide: http://www.chinariders.net/showthread.php?t=20331
2018 Hawk 250 - Full Mod list here. http://www.chinariders.net/showpost....62&postcount=1
2024 Royal Enfield Shotgun 650
https://chinariders.net/showthread.php?t=34124


 
Reply With Quote
Old 03-31-2018, 06:40 PM   #5
BMF   BMF is offline
 
Join Date: Mar 2018
Posts: 24
It's a Mikuni and thank you. I have been watching too many YouTube videos, i think.

I was going to shim the needle but I can get that little tiny clip out. It's not the butterfly style but circular.

Right now I have stopped because I am lost. originally I was losing power with the stock carb at 3/4 throttle. I bought the Mikuni, replaced the main jet to 110 and all seemed good. After I left the bike shop today, it started to cut out and I would get a loud popping sound.

I tried the 100, 105, 110 (the best so far) and now have the 115. From what you are telling me I need to adjust either the small jet or needle. This may be beyond me. I work on servers for a living and find that easier. One and zero's...one and zero's...(server term)


 
Reply With Quote
Old 03-31-2018, 06:51 PM   #6
Megadan   Megadan is offline
 
Megadan's Avatar
 
Join Date: Apr 2017
Location: Omaha, NE
Posts: 8,032
Best thing to do would be to start from a square one baseline.

Intake and exhaust mods? What is your elevation?
__________________
Hawk Information and Resource guide: http://www.chinariders.net/showthread.php?t=20331
2018 Hawk 250 - Full Mod list here. http://www.chinariders.net/showpost....62&postcount=1
2024 Royal Enfield Shotgun 650
https://chinariders.net/showthread.php?t=34124


 
Reply With Quote
Old 03-31-2018, 08:49 PM   #7
BMF   BMF is offline
 
Join Date: Mar 2018
Posts: 24
I just discovered the gasket was ripped for the bowl on the Mikuni. So I took my stock carb, Dremeled the bolts so i could open it with a screwdriver, added a new jet, put everything back together and it works.

The stock carb was good but would crap out at 3/4 throttle. Hopefully the bigger jet will fix that and all will be good. I still need to test drive it. My neighbors have endured enough loudness for the day.

I am at 300 ft elevation. I have been following MotoCheese on YouTube because he is in CT and I am in NH. Pretty much the same elevation.

Thanks for your help!


 
Reply With Quote
Old 04-01-2018, 01:22 AM   #8
Megadan   Megadan is offline
 
Megadan's Avatar
 
Join Date: Apr 2017
Location: Omaha, NE
Posts: 8,032
I was going to link you to that seal, but I keep running into no results.

This is supposed to be what you need, but they are unavailable anywhere. https://www.aliexpress.com/item/Pit-...652507296.html

Hopefully they will show up again.

The other option is to use fuel resistant RTV to seal the bowl, but you will need to run a small consistent bead, let it almost dry, and then put the bowl back on. This will make the bowl a huge pain in the ass to get off again though.
__________________
Hawk Information and Resource guide: http://www.chinariders.net/showthread.php?t=20331
2018 Hawk 250 - Full Mod list here. http://www.chinariders.net/showpost....62&postcount=1
2024 Royal Enfield Shotgun 650
https://chinariders.net/showthread.php?t=34124


 
Reply With Quote
Old 04-01-2018, 11:47 AM   #9
Ariel Red Hunter   Ariel Red Hunter is offline
 
Ariel Red Hunter's Avatar
 
Join Date: Jun 2016
Location: akwesasne, NY-13655
Posts: 2,220
Quote:
Originally Posted by BMF View Post
It's a Mikuni and thank you. I have been watching too many YouTube videos, i think.

I was going to shim the needle but I can get that little tiny clip out. It's not the butterfly style but circular.

Right now I have stopped because I am lost. originally I was losing power with the stock carb at 3/4 throttle. I bought the Mikuni, replaced the main jet to 110 and all seemed good. After I left the bike shop today, it started to cut out and I would get a loud popping sound.

I tried the 100, 105, 110 (the best so far) and now have the 115. From what you are telling me I need to adjust either the small jet or needle. This may be beyond me. I work on servers for a living and find that easier. One and zero's...one and zero's...(server term)
It's not that difficult to change the pilot jet in a Mikuni. It is the other obvious brass piece in the flat bowl, quite near the main jet. I like to use the pilot jet that allows the idle screw to be at 1 1/2 turns out for a good idle. Then, when you have a rich enough main jet, you tune the mid-range by raising (to richen), or lowering the needle....ARH


 
Reply With Quote
Old 04-03-2018, 02:22 PM   #10
BMF   BMF is offline
 
Join Date: Mar 2018
Posts: 24
It's being fixed at a local shop. I had my buddy who is a bike mechanic come by and check it and he says it's something beyond the carb. I will post the results when I get it back. I used the stock and Mikuni and got the same results.


 
Reply With Quote
Old 04-03-2018, 02:25 PM   #11
JerryHawk250   JerryHawk250 is online now
Moderator
 
JerryHawk250's Avatar
 
Join Date: Oct 2016
Location: Houma, La.
Posts: 11,574
Have you adjusted the valves yet? They usually come too tight from the factory.
__________________
2023 Lifan Lycan 250 Chopper
2023 Venom Evader
2022 Lifan KPX250
2020 Kawasaki Vulcan S
2004 Honda ST 1300
2016 Black Hawk 250 (sold)
Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster
2016 Cazador180 XL
2014 Coolster150
JerryHawk250.com
My YouTube Channel


 
Reply With Quote
Old 04-03-2018, 02:42 PM   #12
BMF   BMF is offline
 
Join Date: Mar 2018
Posts: 24
I haven't even made it that far yet. I think it only has 56 miles on it. I just wanted to fix the 3/4+ throttle cutting out. That and the extremely low idle. idle is fixed but the mid to full throttle dies.

I will be fixed soon and then hopefully I can finally ride.


 
Reply With Quote
Old 04-03-2018, 02:52 PM   #13
JerryHawk250   JerryHawk250 is online now
Moderator
 
JerryHawk250's Avatar
 
Join Date: Oct 2016
Location: Houma, La.
Posts: 11,574
Valves being to tight will cause a lot of tuning issues. That should be one of the first things you should do. Many on here can confirm that. Mine had no play what so ever from the factory and the idle was all over the place. Once the valves were adjusted it idles smooth. Something worth checking.
__________________
2023 Lifan Lycan 250 Chopper
2023 Venom Evader
2022 Lifan KPX250
2020 Kawasaki Vulcan S
2004 Honda ST 1300
2016 Black Hawk 250 (sold)
Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster
2016 Cazador180 XL
2014 Coolster150
JerryHawk250.com
My YouTube Channel


 
Reply With Quote
Old 04-03-2018, 03:20 PM   #14
JerryHawk250   JerryHawk250 is online now
Moderator
 
JerryHawk250's Avatar
 
Join Date: Oct 2016
Location: Houma, La.
Posts: 11,574
Here's a good tutorial on valve adjustment. You can skip the steps on removing the tank as you can do it without removing the tank. https://www.cscmotorcycles.com/Articles.asp?ID=293
__________________
2023 Lifan Lycan 250 Chopper
2023 Venom Evader
2022 Lifan KPX250
2020 Kawasaki Vulcan S
2004 Honda ST 1300
2016 Black Hawk 250 (sold)
Keihin PE30 carb,125 main,38 slow.Pod filter,ported & decked head 10:1 CR,Direct Ignition Coil,15/40Sprockets,NGK DPR8EIX-9,De-Cat,Dual Oil Cooler,Digital Cluster
2016 Cazador180 XL
2014 Coolster150
JerryHawk250.com
My YouTube Channel


 
Reply With Quote
Old 04-03-2018, 05:40 PM   #15
Ariel Red Hunter   Ariel Red Hunter is offline
 
Ariel Red Hunter's Avatar
 
Join Date: Jun 2016
Location: akwesasne, NY-13655
Posts: 2,220
Quote:
Originally Posted by BMF View Post
I haven't even made it that far yet. I think it only has 56 miles on it. I just wanted to fix the 3/4+ throttle cutting out. That and the extremely low idle. idle is fixed but the mid to full throttle dies.

I will be fixed soon and then hopefully I can finally ride.
I would not be surprised if you have a vacuum leak causing this problem. Often people over-tighten the carb bolts when re-installing the carburetor. This distorts the flange of either the carb or the intake pipe, allowing vacuum leaks. After that, the next likely culprit is the intake pipe itself. They crack easily from too enthusiastic jiggling and wrenching....ARH


 
Reply With Quote
Reply



Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -4. The time now is 06:10 PM.


Powered by vBulletin® Version 3.8.4
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.